Friday 2 April 2010

CU + PLA

Vik Olliver asked for a volunteer with a heated bed to see if we can extrude onto copper clad board. I didn't think it would stick, but gave it a go anyway.

I first tried ABS onto double sided copper clad FR4 taped to a bed at 120°C. The ABS stuck well enough to extrude the first layer of a 20mm square, but when it cooled down it had no adhesion at all.

PLA at 55°C did exactly the same, but PLA at 130°C stuck very well, so well in fact that I can't get it off with my fingers (the blob was where I aborted the print after the first layer).



Maybe ABS would stick in the same way at an even higher temperature, but maybe not as it is less like glue than PLA. The 120°C / 55°C temperatures are what I use for Kapton, which is why I used them as the starting point.
An interesting aside: I had to measure the PCB to work out the z-height. It is only 1.4mm thick, whereas a standard PCB is 1.6mm. You can also see the grains in the FR4 showing through the copper. This means the board I bought in Maplin for home PCB use is actually the same stock material that they use for the first part of a commercial production process, but when they plate thorough the vias they increase the thickness of the copper all over to get the standard 1oz/inch2. I don't know if this is always the case, i.e, that all home made PCBs have less copper than a production one, or whether you can get bare board with 1oz on it already.
Anyway a good result, assuming PLA will resist PCB etchant. Also, it seemed like a potential bed technique. I.e. do the first layer onto hot copper and then cool it to about 50°C for the rest of the object. I tried it with this butterfly: -



It worked perfectly. After the first layer I blew it with a fan to cool it down to 50°C. It took about four layers to get down to that temperature. Since I added the insulation under the bed it takes longer to cool it than it does to heat it.

After it had finished and cooled down to 40°C it was still firmly attached, so I removed it by flexing the PCB.



The base of the object is perfectly flat.



I think for PLA this might be a better technique than Kapton. I can't imagine the PCB wearing out. It could also be self heating with a serpentine track on the other side. I don't know that just taping it down would be strong enough for making large objects. I could solder fastenings on the back if not.

I don't know if there is anything special about copper and PLA, or whether other hot metals and plastic would work . I tried similar things with ABS on AL, but may not have had it hot enough.

Thursday 25 March 2010

Heated bed MK3

My first heated bed worked OK but it was slow to warm up and hard to remove objects.



The second one was only ever intended for experimenting with vacuums and magnets but I ended up printing most of my Mendel on it. It worked well but limits the build area.



I have now replaced it with a full size version, using the lessons learned from the first two.

The first bed was the same size as HydraRaptor's table (200 × 200mm) but the build area is only about 150 × 150mm. The warm up time and power are both proportional to area, so I made this one just big enough, i.e. 150×150mm. Removing the 25mm border nearly halves the area!

The other innovations were to make it easier to build. I replaced nine AL clad resistors with four TO220 resistors. These are rated at 50W and 155°C, so are actually totally within spec when I run the table from 48V giving 188W. Instead of having to tap two M2 holes for each resistor these only need a single M3 hole. That is much easier to tap as the tap is a lot sturdier.



They are also lower profile of course. I just noticed that 47Ω ones are less than half the price, so I should have used four of those in parallel instead.

The thermocouple is mounted with a clamp made from PTFE.

Since this bed has a steel plate on top none of the holes need to be blind. That makes drilling and tapping easier as well.

On my previous magnetic bed I placed the magnets in blind holes that were almost all the way through. That required a milling machine to get flat bottomed holes. On this version I just drilled almost all the way though, leaving a lip to retain the magnet.



This is the top side. The magnet in the middle was done with an alternative technique. I drilled a through hole and then jammed the magnet in with a few strands of copper wire. That gets it flush with the surface, giving maximum magnetic force, but it pulled through on first use. I will have to glue it with high temperature epoxy I think.



After a suggestion by Enrique that wool was a good high temperature insulator my friend Steve gave me some carpet underlay made from wool. I used it to insulate the underside, thanks guys.



For the steel plate on the top I used the cover of an old CD ROM. It is only 145mm wide unfortunately. I think it is mild steel with nickel plating. Not as good as the stainless steel springy piece I got from inside a toaster.

So here is the finished article with the biggest bit of Mendel built on it. It was quite hard to remove. I had to remove the steel plate and bend it a little as intended. I had found that things I built recently on the small table could be removed without lifting the plate. I think the Kapton gets less grip as it ages. I tried cleaning it with alcohol and sanding it with very fine emery paper, but that seemed to make it worse if anything. It seems that shiny Kapton gives more grip than matt.

Sunday 21 March 2010

Making Mendel

I aimed to build my Mendel in time to show it at the Makerfaire in Newcastle but completely failed. I had two weeks to build it, which I thought was plenty. In actual fact it took closer to three weeks before I got it printing successfully. I had no major problems, just a few snags here and there and a severe underestimation of how long it would take on my part.

Printed Parts

Unlike when I printed two sets of Darwin parts, printing the parts was the easy bit. This was due to three breakthroughs I had at the beginning of the year: -
  • The heated Kapton bed removed the need for rafts, which not only take a significant time to print, but also can take a lot of manual work to remove.
  • The extruder fast reverse got rid of all the strings, which also took a long time to clean up, especially from inside the Darwin corner blocks.
  • The "no compromise" extruder is so reliable that I have the confidence to do multi-part, layer by layer builds, which gets a lot more on the table, allowing longer unattended operation.


I printed the parts with 0.4mm or 0.375mm filament and with 25% infill. For the larger parts I used two outlines for strength. Since the large parts don't need fine detail, I think printing them with 0.5mm filament and one outline would be quicker, but that would need a bigger nozzle.

The weight of the parts, not including the extruder, was only 730g. I printed the outlines at 16mm/s and the infill at 32mm/s, so it's hard to say the total time. Assuming an average speed of 24mm/s at 0.4mm diameter gives about 3 mm3/s. That would put the total time at about 65 hours. I did it as a background task over a few weeks. A lot of the parts were printed as experiments with heated beds.

Rods

I took me an evening to cut all the rods. The method I used was to nail a stop to my workbench to line up the rod against a metre rule.



I then lined a piece of masking tape up with the correct measurement and wrapped it round the rod to mark the place to cut. I also wrote the name of the rod on the tape to make it easy to identify later.



A Black & Decker workmate makes an ideal vice to hold the rods while sawing. I rotate the studding until the thread lines up with the edge of the masking tape. That guides the saw to start in exactly the right place.



I used BZP for all the studding except the z-leadscrews, for which I used A2 stainless steel because it is smoother and generally straighter. I bought the rods from Farnell and even the BZP studding was very straight, a lot better than the stuff you get in B&Q. I also used A2 for all the bars.

It was very hard work sawing the A2 until I switched to a new blade and used Trefolex cutting compound. I am not sure which made the most difference, but I could then cut the A2 much easier than I had been previously cutting the BZP. I wish I had done that earlier, it would have saved a few hours.



Thick Sheets

The thick sheet parts are not really suitable for making by hand, particularly the squashed frog. They have lots of slots, which are hard to make without a milling machine or a laser cutter, etc.



I am not sure exactly what the hole in the bed and the purge plate are for, so I made the bed a simple rectangle with four holes. I am using my own electronics, so I made the two circuit board plates to suite. I simply cut rectangles and I marked the holes and drilled them in the right place, so no need for slots. That just left the squashed frog.

I made a much simpler design with drill centres on it. There is no need for the bulging legs and sloping shoulders. I think they must be just to make it look more like a frog. Fine if you you are CNCing it, but a PITA if you have to make it by hand. Also the holes for the opto tab and the purge plate are mirrored for no apparent reason, so I made it chiral.



This just starts as a rectangle with some holes in it. Then the large slots are made with a saw thin enough to turn in the holes. The outer holes that mount the bearings can be round because they are in a a fixed place, dictated by the holes in the bed. The inner holes need to be slots because the bearings are adjustable. I just left them off the template and marked them with the bearings adjusted and in place.



I made the sheets from 3mm Dibond, which is below the recommended thickness, but seems stiff enough. It is also light weight and very easy to machine.

Thin Sheet

I didn't have any optos, so I used micro switches for my end stops, hence didn't need any thin sheet parts. I simply attached them to the bars of each axis with P-clips. A little RepRapped bracket would be better but I was building this in a hurry, so had gone into bodging mode at this point!







They seem to have sufficient repeatability and certainly will when I replace the electronics with my new design, which will know the motor phase, reducing the uncertainty by a factor of 32. It is the same switch that I have used on the z-axis of HydraRaptor, which has proven totally reliable. They seem to be this one from RS, not cheap.

Belts

These were easy enough to split but, because the reinforcing wires run in a spiral, the blade tends to follow one for a while before managing to cut through it. That leaves a ragged edge with a bit of wire sticking out.

I didn't understand the rationale for slackening the belts until you just don't see backlash when moving one motor detent. I am microstepping anyway, so a motor detent is not significant. I made my belts good and tight.

Snags

I had a few snags with the mechanical assembly: -

The x-axis spacers are too short. The STL files are 5mm shorter than the parts in the STEP assembly. That caused the motor to clash with the nuts on the 360 bearing.



The 180 bearing at the other end was about 10mm from where it should be.



A simple fix was to slide the axis along leaving a 10mm gap to the spacer, the only problem remaining is that the spacers rattle at certain step rates.



The STEP model shows this gap should be only 5mm, but I have been unable to find the discrepancy. My rods and inspection distances are correct and the ends of the rods are flush with the clamps, as they are in the model.

The bed springs seemed to be too long to compress to the length of the bed-height-spacer-31mm_1off, which is not actually 31mm, but 29mm, so I don't know what gives there, I just spaced them a bit higher.



The bolts in the z-bar clamps are too long to allow the bearing to be inserted. I replaced them with shorter ones.



Similarly the bolts in the x-carriage get in the way of the extruder I fitted.



The J3 jigged distance did not seem correct. The distance between the y-bars is set by the J2 distance and the 3 nut spacers.

Extruder

I used Wade's extruder design as I didn't have time to adapt any of my own.



The gears work well, with very little backlash, but the small one has some movement on the motor shaft. It is just a press fit with a flat on the shaft. I need to redesign it with a captive nut and grub screw.

I didn't have a suitable M8 shoulder bolt so I made one from brass by attaching a nut with a pin through it.



I hobbed it with an M3.5 tap. I haven't measured the grip, but I get the impression it is not as high as Wade gets, I am not sure why.

For the bottom half of the extruder I used some parts that Brian was looking for volunteers to test for him.



The insulator is made from PEEK with a PTFE liner. The idea being to get the strength of the PEEK and the slipperiness of the PTFE. It seems to work well with PLA, which is all I have run through it so far.

The barrel is long because it is designed to take nichrome, but I just screwed it into a block of aluminium with a vitreous enamel resistor in it.



This was left over from a previous experiment. I have now moved onto a smaller resistor size, so this block could be smaller. The barrel could be a lot shorter with this arrangement and that would give less ooze and less viscous resistance.

The extruder works well with PLA. The main problem with it is that it mounts at right angles to the x-axis, so the motor severely restricts the maximum height of the z-axis. Another issue is that to remove it you have to remove the motor to get at the bolts. To remove the motor you have to remove the big pulley to get at the motor's bolts, to do that you have to remove the pinch wheel assembly. I.e. to remove the extruder you have to completely disassemble it!

Electronics

To get up and running quickly I used the same electronics that I use on HydraRaptor. The only difference being that I used MakerBot V3 stepper drivers. These use the A3977 chip and give x8 microstepping. That gives an axis resolution of 0.025mm, but more importantly gives nice smooth running.

When the weather was exceptionally dry I found they are very sensitive to static. A discharge to any part of the machine would cause the A3977 to shut down its outputs and draw enough current from the 5V rail to cause the 100mA regulator to current limit. The red LED on the power rail goes dim. Powering off and on again fixes it and there doesn't seem to be lasting damage. I suspect that might not be the case if the 5V rail was not current limited. Apparently the only way to fix it is to add external Schottky diodes. That is very disappointing as one of the nice features of the chip is that it is supposed not to need them. I will investigate further to see if all eight diodes are needed before making my own board.

Firmware

I used the same firmware as HydraRaptor. I just added some compile time conditionals to cope with two pin outs and a different IP and MAC address for each machine. I also had to change from 16bit to 32 bit positional commands because the axes are bigger.

Software

I used the same Python software as HydraRaptor but I had to re-factor it quite a lot to support both machines. I added a class to represent the Cartesian bot which holds the axis resolution, direction, maximum speed and acceleration plus the IP address. I also added a class to represent the extruder controller as I have calibration values unique to each board. I already had classes to represent thermistors and extruders.

I can run both machines at the same time from one PC and, because I only use the Skeinforge output for the toolpath, I can use the same sliced files for either machine. This is despite the fact that they run at different speeds and are loaded with different plastic.

Results

So here is the finished machine: -



And here is a video showing it being tested: -


I am running the X & Y motors at about 0.75A and Z at about 1A. I have set the maximum XY speed to 100mm/s, but I think it could go a lot faster. Z only goes at about 5mm/s because not only is it a threaded rod drive, but it is geared down by the belt and pulleys!

I haven't printed a lot yet, but so far the results look as good as they do from HydraRaptor. The next thing to do is add a heated bed and try ABS.