Monday, 9 August 2010

Rejuvenated Bed

I put new PET tape on my heated bed at the beginning of July. Since then I have printed 15 Mendels on it, but on the last few I was getting problems with the parts not sticking. That is after about 700 hours of printing and ~15kg of plastic. I occasionally swab it down with Isopropanol to remove grease from finger prints, but Isopropanol is not a solvent for ABS. This evening I tried cleaning it with acetone instead. It dramatically increased the grip level, restoring it to new and making the parts hard to remove again! ABS must leave some traces behind on the surface of the bed and the acetone removes it.

So it looks like PET tape is almost fully reusable. It tends to get the odd blister where the corners of big objects overcome its adhesive and picks up a few scars from the odd accident with a knife. Apart from that it just needs cleaning with acetone about once a month.

Monday, 19 July 2010

A bit of a drag

One problem I have had, on and off, with Mendel is a tendency for the infill not to meet the outline. This was particularly bad with PLA. I have combated this by having some infill overlap and also extruding the plastic slightly faster than it should be, so that the solid layers are well stuffed. I don't have to do either of these things with HydraRaptor. I couldn't figure out what the difference was until I changed a reel of plastic recently. The first print on the new reel came out like this: -



The gap is always at one side like this, it is as if the infill is not centred within the outline. The reason, I have come to realise, is that the belt has some play in it because it is not infinitely taught. When the extruder pulls filament off a reel it exerts a force on the carriage, which displaces it slightly from where it would come to rest without any external force. Because the carriage moves, the filament only gets pulled from the reel at the local extremes of movement, the rest of the time it is slack. This causes small offsets in the filament paths. In particular, when it is doing zigzag infill it is using filament relatively quickly, so at the end of the zigzag furthest from the centre of the bed it is likely to give a little tug of the reel each time, causing the zigzag to stop short of the outline.

The conclusion is that the filament feed for a belt-driven moving-head machine needs to be very low drag. The hanging basket technique that I used on HydraRaptor is no good because it has to pull plastic out from under its own weight. Making the feed point high above the machine reduces the lateral drag on the carriage, but you can easily get enough vertical drag to deflect the x-bars upwards, or even lift the z-axis slightly because the backlash in the thread is only taken up by the weight of the x-axis.

The reason it was bad with PLA was because I was pulling it from a hanging basket and being very stiff, even a small coil needs a lot of tug.

The system I now use is a vertically mounted spool big enough to take 5kg coils, which last me a couple of weeks.



The bearing is just a stainless steel axle running in PLA bushes, lubricated with some lithium grease. It is low friction, but not as frictionless as a ball bearing. It needs a little friction to stop any in-balance in the coil causing the spool to spin to its low point. Also the faces of the spool need to be quite big to stop a loose loop of filament coming over the side. It pulls tight and jams if that happens.

I can take the spool apart to insert a new coil of plastic.



In general though I have to wind it all off and on again to get it tight and balanced enough to wind off smoothly. Since 5kg is about 800m it takes a long time to wind it onto a garden hose reel and then back on again. Someday I will get round to making a machine to do it for me. In the meantime I will make a second identical spool so that I can just mount the coil on one spool and wind it onto a second one to use.

Thursday, 8 July 2010

Meltdown

While making its 18th child, my Mendel made a real pig's ear of laying down the first layer holes at the start of a build. So bad that the infill did not join to them and started curling upwards. I had to watch it a while before I realised what the problem was. The extruder had come loose and was bouncing up and down when the filament feed stopped and started.

I thought it was just that the bolts had worked loose but after I tightened them it was still moving and there were some worrying crunching sounds, so it was time to strip it down.


The bottom of the heatsink is covered with a sticky deposit. It is some volatile component that boils off the ABS and condenses on cold surfaces,



The main extruder bracket had broken and the carriage didn't look too good either: -



I stripped the carriage down as well and found that it was cracked and severely distorted.



The main problem I realised is my modified hot end. Normally the insulator is locked into the chunky part of the bracket by a couple of M3 bolts through it. I can't get those in because my heatsink is in the way, so I rely on the mounting bolts and the upper carriage to take the extrusion force. On reflection, not a good idea!



The lower carriage is less deformed because the extrusion force does not pass though it.



The heat rising from the bed and the extruder must be enough to soften the carriage and let it deform, but also it seems to have made the ABS weak and crumbly. Even the belt clamps have deformed.



This is after about 3 months of printing though so it isn't a big problem to replace them as long as you have spares. I had just printed a carriage before it failed so it was easy to replace but I had to print another extruder on HydraRaptor. You really need to have a full set of spares on hand, or have two machines.

I did various changes to make it more durable. The main thing is I fitted nuts under the heatsink so that no force goes through the carriage. I also put large penny washers on the top of the extruder bracket to reinforce the lugs. Ideally they should be a bit thicker but that would reduce the Z travel even further. The extruder motor clashes with the frame which reduces the height. Then my heatsink loses another 10mm or so and my heated bed loses 26mm. I am left with about 35mm which is only just enough to build the tallest Mendel part (the lower carriage).

I also used nyloc nuts in the captive positions in the carriage. The wiki advises against this as it may crack the plastic but it doesn't seem to be case with my ABS parts. Ordinary nuts don't stay tight because the plastic creeps.





I intend to fit some sort of heat shield to stop the heat rising from the bed reaching the carriage. In the mean time I have started fitting the front on my cabinet after the first layer is finished, when the bed temperature drops from 140°C to 110 °C. That can be up to 90 minutes into the build, so not convenient.