Thursday 10 April 2008

More PLAying

The tweaks I made to my extruder dramatically improved its ability to extrude PLA. I am not sure which one made all the difference or whether they are all needed. I can now extrude at my target 0.5mm filament 16mm/s with about 75% motor PWM duty cycle. That is less than I needed for ABS before the tweaks.

I can also extrude at lower temperatures. I think 180°C is a bit on the hot side as the plastic is very runny at the temperature. It will flow out of the extruder under gravity and has negative die swell. At 140°C it behaves more like the other plastics and swells to 0.6mm, which is very low.

In a previous article I stated that I could not make sparse filled objects because the filament slumped too much. With the reduction in temperature and increase is speed I now can. Here is a 50% filled block: -



It is still very strong. I expected the warping to be less but I have switched from MDF to balsa and I think that increased it. The balsa I have is only 2mm thick and was only stuck down with masking tape. I might try gluing two pieces back to back with the grains at right angles to get it stiffer.



So now with a slightly tweaked extruder I can do PCL, PLA and ABS at 0.5mm @ 16mm/s. I had to slow down for HDPE to prevent thermal damage to the extruder.

To get good definition at high speed I extrude with a fan running. The fan cools the nozzle which causes more heater power so the barrel temperature rises to the point where PTFE goes soft and the JB Weld turns to dust. PCL and PLA are no problem because the temperature is less. ABS does not seem to need the fan.

I plan to make a PTFE cover for the nozzle which will probably insulate it well enough and hopefully stop filament sticking to it and burning.

Tuesday 8 April 2008

Fantastic PLAstic

I have managed to get the GM3 to extrude PLA reliably with the following tweaks: -
  • I locked the clutch as per Solarbotics instructions.
  • I lubricated the GM3 with silicon grease as per Adrian Bowers suggestion.
  • I sharpened the thread a bit with a half round file following Vik Olliver's instructions.
  • I spaced the top half of the pump slightly further apart with some thicker washers. That gives the thread a gentle lead in.
  • Plenty of oil on the filament.
  • I throttled back the flow rate to 3/4 of the rate I normally use (π mm3/s).
The motor runs warm, but not alarmingly so. For some reason the filament is no longer rotating in the extruder.

My first attempt curled away from the MDF bed so I used 2mm balsa wood as Adrian has been using for PCL. That worked well so it's good that we can use it for both. I have yet to try it with HDPE and ABS.

I made my standard test block with 0.5mm filament extruded at 180°C (at the nozzle), layer height 0.4mm, pitch 0.6mm, fan on constantly. The results are excellent: very good filament compliance, i.e. sharp corners and flat sides, excellent layer bonding.

It is slightly more warped than my first test. That is probably because balsa is softer than MDF.



No warts on this one!

Monday 7 April 2008

Locking the Solarbotics GM3 clutch

All the adverts for the Solarbotics GM3 gearmotor say the clutch can easily be locked but don't say how. I emailed them today and got a quick reply from Dan: -
Locking the clutch is actually very easy... we should make an effort to get the instructions on-line. All you have to do is glue the little plastic clutching mechanism in its cavity, but to ensure a good contact you should first wipe it out with rubbing alcohol to get the grease out, then score the surface up a bit with the tip of an Exacto knife and then you can use either super glue, model cement, or epoxy to lock it.
So that is what I shall try next to see if i can get it to extrude PLA without warts.