Having assembled and dismantled my extruder a few times I found it quite fiddly and time consuming. The reason being is that all the fasteners need either an Allen key and a spanner or two spanners. I solved this by placing shake proof washers between the screw heads and the plain washers that are there for load spreading. Only problem was I had to buy them in packs of 250 so I have enough to last the rest of my life!
The result is that once the bolts are finger tight the washers bite and hold the head so only one spanner is required to tighten the nuts.
The nuts that tighten the springs were still a bit tedious. This is because they need tightening a long way down the thread to tension the spring and you need a spanner all the way because the springs are stiff. Wing nuts are the obvious answer but I didn't have any and I am not sure whether there is room to spin them. Instead, I milled some knobs out of Perspex and tapped them to act as nuts. I have christened them knobby nuts but that probably only strikes a chord with people in the UK.
Thursday, 9 August 2007
Tuesday, 7 August 2007
Roll out the barrel
I don't seem to have achieved much in the last week as I have been waiting for a few things to arrive. I have managed to mount the extruder on the bottom bracket that previously held the milling drill. I had planned to do that to make it easy to swap between the two, so I used a smaller diameter PTFE rod for the thermal barrier to allow it to fit through the same hole as the drill. What I forgot was that the wires would also have to pass through the same hole! It is a tight squeeze as you can see. The heater wires actually have some plastic insulation where they pass through the aluminium, I hope it doesn't melt!
Another thing I forgot to allow for is that I had to mount the extruder clamp on standoffs to clear the bolt heads and leave space for the wires to exit. Unfortunately that means the nozzle doesn't quite reach the XY table so whatever base material I decide to extrude onto will have to be at least 5mm thick.
On the left of the nozzle you can just see a small thermistor to measure its temperature. The recommended part from RS is on back order but one of my fellow reprappers called englewood was kind enough to send me the alternative one you can see. I hope to repay him with some HDPE extruder parts if my machine is successful at making them.
I attached it by filing a flat on the barrel and clipping it with a couple of coils cut from a small spring. I used a little thermal grease between the two.
The next step is to calibrate the thermistor and see if it will extrude.
Another thing I forgot to allow for is that I had to mount the extruder clamp on standoffs to clear the bolt heads and leave space for the wires to exit. Unfortunately that means the nozzle doesn't quite reach the XY table so whatever base material I decide to extrude onto will have to be at least 5mm thick.
On the left of the nozzle you can just see a small thermistor to measure its temperature. The recommended part from RS is on back order but one of my fellow reprappers called englewood was kind enough to send me the alternative one you can see. I hope to repay him with some HDPE extruder parts if my machine is successful at making them.
I attached it by filing a flat on the barrel and clipping it with a couple of coils cut from a small spring. I used a little thermal grease between the two.
The next step is to calibrate the thermistor and see if it will extrude.
Tuesday, 31 July 2007
Hotting up
The latest RepRap heater design consists of insulated nichrome wire wound around a threaded barrel and then stuck down with a coating of J-B Weld high temperature epoxy. I think that is a good way to do it but the insulated nichrome is expensive and I happen to have some nichrome from a heating element. It came from an old hair dryer I think.
Luckily it seems to be the right gauge to give me a reasonable number of turns. The spec was for 8 ohms which gives a maximum wattage of 18W at 12V. That gave me a length of about 340 mm which made 17 turns. I attached some tinned copper tails to make the connections easier to handle. I tied them to the nichrome and then soldered it. On reflection that was probably a bad idea as the solder does not stick to nichrome so if it oxidizes it may go open circuit. Small crimps would be a better I think.
I started by laying down a layer of J-B Weld to insulate the barrel.
After letting this dry for 24 hours I put it in the lathe and turned it down to as thin a layer as I could get before it started flaking off. That was at about 0.2mm.
I added some more J-B Weld to repair the gaps and also used it to attach one end of the nichrome.
After another 24 hours I put it back in the lathe to make the winding.
Finally I added another thick layer of J-B Weld and left it another 24 hours to set. A very slow way of doing it compared to using insulated nichrome and a single coat of J-B Weld.
I tested it by putting a thermocouple probe down the barrel and running it from a variable bench power supply. I heated it up to 200 °C at which point it smoked a bit and the J-B Weld started to discolour. I dropped it back down to 160 °C which only required about 5W of power and pushed some HDPE filament down it. Pressing as hard as I could I got it to extrude some 0.75mm diameter filament though the 0.5mm hole in the nozzle. You can just see a little bit poking out in the picture of the finished article below :-
I don't know how long it will last, the J-B Weld may crack as there is nowhere for the nichrome to expand to. Insulated nichrome would be better in this respect.
There should also be a glass bead thermistor attached to the nozzle to monitor the temperature so that it can be regulated in software. Having seen the resistance of copper stepper motor coils increase noticeably when they get hot, and tungsten light bulb filaments change resistance by a factor of ten, I thought I should try using the resistance of the heater to measure its temperature. The resistance didn't seem to change much so I looked up the temperature coefficient and found it was much lower than other metals, so that is a non starter. I have ordered a couple of thermistors but they are out of stock at the moment so I will have to run it open loop to start with.
The next thing to do is put the pump back together and see if it can extrude.
Luckily it seems to be the right gauge to give me a reasonable number of turns. The spec was for 8 ohms which gives a maximum wattage of 18W at 12V. That gave me a length of about 340 mm which made 17 turns. I attached some tinned copper tails to make the connections easier to handle. I tied them to the nichrome and then soldered it. On reflection that was probably a bad idea as the solder does not stick to nichrome so if it oxidizes it may go open circuit. Small crimps would be a better I think.
I started by laying down a layer of J-B Weld to insulate the barrel.
After letting this dry for 24 hours I put it in the lathe and turned it down to as thin a layer as I could get before it started flaking off. That was at about 0.2mm.
I added some more J-B Weld to repair the gaps and also used it to attach one end of the nichrome.
After another 24 hours I put it back in the lathe to make the winding.
Finally I added another thick layer of J-B Weld and left it another 24 hours to set. A very slow way of doing it compared to using insulated nichrome and a single coat of J-B Weld.
I tested it by putting a thermocouple probe down the barrel and running it from a variable bench power supply. I heated it up to 200 °C at which point it smoked a bit and the J-B Weld started to discolour. I dropped it back down to 160 °C which only required about 5W of power and pushed some HDPE filament down it. Pressing as hard as I could I got it to extrude some 0.75mm diameter filament though the 0.5mm hole in the nozzle. You can just see a little bit poking out in the picture of the finished article below :-
I don't know how long it will last, the J-B Weld may crack as there is nowhere for the nichrome to expand to. Insulated nichrome would be better in this respect.
There should also be a glass bead thermistor attached to the nozzle to monitor the temperature so that it can be regulated in software. Having seen the resistance of copper stepper motor coils increase noticeably when they get hot, and tungsten light bulb filaments change resistance by a factor of ten, I thought I should try using the resistance of the heater to measure its temperature. The resistance didn't seem to change much so I looked up the temperature coefficient and found it was much lower than other metals, so that is a non starter. I have ordered a couple of thermistors but they are out of stock at the moment so I will have to run it open loop to start with.
The next thing to do is put the pump back together and see if it can extrude.
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