My first heated bed worked OK but it was slow to warm up and hard to remove objects.
The second one was only ever intended for experimenting with vacuums and magnets but I ended up printing most of my Mendel on it. It worked well but limits the build area.
I have now replaced it with a full size version, using the lessons learned from the first two.
The first bed was the same size as HydraRaptor's table (200 × 200mm) but the build area is only about 150 × 150mm. The warm up time and power are both proportional to area, so I made this one just big enough, i.e. 150×150mm. Removing the 25mm border nearly halves the area!
The other innovations were to make it easier to build. I replaced nine AL clad resistors with four TO220 resistors. These are rated at 50W and 155°C, so are actually totally within spec when I run the table from 48V giving 188W. Instead of having to tap two M2 holes for each resistor these only need a single M3 hole. That is much easier to tap as the tap is a lot sturdier.
They are also lower profile of course. I just noticed that 47Ω ones are less than half the price, so I should have used four of those in parallel instead.
The thermocouple is mounted with a clamp made from PTFE.
Since this bed has a steel plate on top none of the holes need to be blind. That makes drilling and tapping easier as well.
On my previous magnetic bed I placed the magnets in blind holes that were almost all the way through. That required a milling machine to get flat bottomed holes. On this version I just drilled almost all the way though, leaving a lip to retain the magnet.
This is the top side. The magnet in the middle was done with an alternative technique. I drilled a through hole and then jammed the magnet in with a few strands of copper wire. That gets it flush with the surface, giving maximum magnetic force, but it pulled through on first use. I will have to glue it with high temperature epoxy I think.
After a suggestion by Enrique that wool was a good high temperature insulator my friend Steve gave me some carpet underlay made from wool. I used it to insulate the underside, thanks guys.
For the steel plate on the top I used the cover of an old CD ROM. It is only 145mm wide unfortunately. I think it is mild steel with nickel plating. Not as good as the stainless steel springy piece I got from inside a toaster.
So here is the finished article with the biggest bit of Mendel built on it. It was quite hard to remove. I had to remove the steel plate and bend it a little as intended. I had found that things I built recently on the small table could be removed without lifting the plate. I think the Kapton gets less grip as it ages. I tried cleaning it with alcohol and sanding it with very fine emery paper, but that seemed to make it worse if anything. It seems that shiny Kapton gives more grip than matt.
Thursday, 25 March 2010
Sunday, 21 March 2010
Making Mendel
I aimed to build my Mendel in time to show it at the Makerfaire in Newcastle but completely failed. I had two weeks to build it, which I thought was plenty. In actual fact it took closer to three weeks before I got it printing successfully. I had no major problems, just a few snags here and there and a severe underestimation of how long it would take on my part.
Printed Parts
Unlike when I printed two sets of Darwin parts, printing the parts was the easy bit. This was due to three breakthroughs I had at the beginning of the year: -
I printed the parts with 0.4mm or 0.375mm filament and with 25% infill. For the larger parts I used two outlines for strength. Since the large parts don't need fine detail, I think printing them with 0.5mm filament and one outline would be quicker, but that would need a bigger nozzle.
The weight of the parts, not including the extruder, was only 730g. I printed the outlines at 16mm/s and the infill at 32mm/s, so it's hard to say the total time. Assuming an average speed of 24mm/s at 0.4mm diameter gives about 3 mm3/s. That would put the total time at about 65 hours. I did it as a background task over a few weeks. A lot of the parts were printed as experiments with heated beds.
Rods
I took me an evening to cut all the rods. The method I used was to nail a stop to my workbench to line up the rod against a metre rule.
I then lined a piece of masking tape up with the correct measurement and wrapped it round the rod to mark the place to cut. I also wrote the name of the rod on the tape to make it easy to identify later.
A Black & Decker workmate makes an ideal vice to hold the rods while sawing. I rotate the studding until the thread lines up with the edge of the masking tape. That guides the saw to start in exactly the right place.
I used BZP for all the studding except the z-leadscrews, for which I used A2 stainless steel because it is smoother and generally straighter. I bought the rods from Farnell and even the BZP studding was very straight, a lot better than the stuff you get in B&Q. I also used A2 for all the bars.
It was very hard work sawing the A2 until I switched to a new blade and used Trefolex cutting compound. I am not sure which made the most difference, but I could then cut the A2 much easier than I had been previously cutting the BZP. I wish I had done that earlier, it would have saved a few hours.
Thick Sheets
The thick sheet parts are not really suitable for making by hand, particularly the squashed frog. They have lots of slots, which are hard to make without a milling machine or a laser cutter, etc.
I am not sure exactly what the hole in the bed and the purge plate are for, so I made the bed a simple rectangle with four holes. I am using my own electronics, so I made the two circuit board plates to suite. I simply cut rectangles and I marked the holes and drilled them in the right place, so no need for slots. That just left the squashed frog.
I made a much simpler design with drill centres on it. There is no need for the bulging legs and sloping shoulders. I think they must be just to make it look more like a frog. Fine if you you are CNCing it, but a PITA if you have to make it by hand. Also the holes for the opto tab and the purge plate are mirrored for no apparent reason, so I made it chiral.
This just starts as a rectangle with some holes in it. Then the large slots are made with a saw thin enough to turn in the holes. The outer holes that mount the bearings can be round because they are in a a fixed place, dictated by the holes in the bed. The inner holes need to be slots because the bearings are adjustable. I just left them off the template and marked them with the bearings adjusted and in place.
I made the sheets from 3mm Dibond, which is below the recommended thickness, but seems stiff enough. It is also light weight and very easy to machine.
They seem to have sufficient repeatability and certainly will when I replace the electronics with my new design, which will know the motor phase, reducing the uncertainty by a factor of 32. It is the same switch that I have used on the z-axis of HydraRaptor, which has proven totally reliable. They seem to be this one from RS, not cheap.
Belts
These were easy enough to split but, because the reinforcing wires run in a spiral, the blade tends to follow one for a while before managing to cut through it. That leaves a ragged edge with a bit of wire sticking out.
I didn't understand the rationale for slackening the belts until you just don't see backlash when moving one motor detent. I am microstepping anyway, so a motor detent is not significant. I made my belts good and tight.
The x-axis spacers are too short. The STL files are 5mm shorter than the parts in the STEP assembly. That caused the motor to clash with the nuts on the 360 bearing.
The 180 bearing at the other end was about 10mm from where it should be.
A simple fix was to slide the axis along leaving a 10mm gap to the spacer, the only problem remaining is that the spacers rattle at certain step rates.
The STEP model shows this gap should be only 5mm, but I have been unable to find the discrepancy. My rods and inspection distances are correct and the ends of the rods are flush with the clamps, as they are in the model.
The bed springs seemed to be too long to compress to the length of the bed-height-spacer-31mm_1off, which is not actually 31mm, but 29mm, so I don't know what gives there, I just spaced them a bit higher.
The bolts in the z-bar clamps are too long to allow the bearing to be inserted. I replaced them with shorter ones.
Similarly the bolts in the x-carriage get in the way of the extruder I fitted.
The J3 jigged distance did not seem correct. The distance between the y-bars is set by the J2 distance and the 3 nut spacers.
The gears work well, with very little backlash, but the small one has some movement on the motor shaft. It is just a press fit with a flat on the shaft. I need to redesign it with a captive nut and grub screw.
I didn't have a suitable M8 shoulder bolt so I made one from brass by attaching a nut with a pin through it.
I hobbed it with an M3.5 tap. I haven't measured the grip, but I get the impression it is not as high as Wade gets, I am not sure why.
For the bottom half of the extruder I used some parts that Brian was looking for volunteers to test for him.
The insulator is made from PEEK with a PTFE liner. The idea being to get the strength of the PEEK and the slipperiness of the PTFE. It seems to work well with PLA, which is all I have run through it so far.
The barrel is long because it is designed to take nichrome, but I just screwed it into a block of aluminium with a vitreous enamel resistor in it.
This was left over from a previous experiment. I have now moved onto a smaller resistor size, so this block could be smaller. The barrel could be a lot shorter with this arrangement and that would give less ooze and less viscous resistance.
The extruder works well with PLA. The main problem with it is that it mounts at right angles to the x-axis, so the motor severely restricts the maximum height of the z-axis. Another issue is that to remove it you have to remove the motor to get at the bolts. To remove the motor you have to remove the big pulley to get at the motor's bolts, to do that you have to remove the pinch wheel assembly. I.e. to remove the extruder you have to completely disassemble it!
Electronics
To get up and running quickly I used the same electronics that I use on HydraRaptor. The only difference being that I used MakerBot V3 stepper drivers. These use the A3977 chip and give x8 microstepping. That gives an axis resolution of 0.025mm, but more importantly gives nice smooth running.
When the weather was exceptionally dry I found they are very sensitive to static. A discharge to any part of the machine would cause the A3977 to shut down its outputs and draw enough current from the 5V rail to cause the 100mA regulator to current limit. The red LED on the power rail goes dim. Powering off and on again fixes it and there doesn't seem to be lasting damage. I suspect that might not be the case if the 5V rail was not current limited. Apparently the only way to fix it is to add external Schottky diodes. That is very disappointing as one of the nice features of the chip is that it is supposed not to need them. I will investigate further to see if all eight diodes are needed before making my own board.
I can run both machines at the same time from one PC and, because I only use the Skeinforge output for the toolpath, I can use the same sliced files for either machine. This is despite the fact that they run at different speeds and are loaded with different plastic.
And here is a video showing it being tested: -
I am running the X & Y motors at about 0.75A and Z at about 1A. I have set the maximum XY speed to 100mm/s, but I think it could go a lot faster. Z only goes at about 5mm/s because not only is it a threaded rod drive, but it is geared down by the belt and pulleys!
I haven't printed a lot yet, but so far the results look as good as they do from HydraRaptor. The next thing to do is add a heated bed and try ABS.
Printed Parts
Unlike when I printed two sets of Darwin parts, printing the parts was the easy bit. This was due to three breakthroughs I had at the beginning of the year: -- The heated Kapton bed removed the need for rafts, which not only take a significant time to print, but also can take a lot of manual work to remove.
- The extruder fast reverse got rid of all the strings, which also took a long time to clean up, especially from inside the Darwin corner blocks.
- The "no compromise" extruder is so reliable that I have the confidence to do multi-part, layer by layer builds, which gets a lot more on the table, allowing longer unattended operation.
I printed the parts with 0.4mm or 0.375mm filament and with 25% infill. For the larger parts I used two outlines for strength. Since the large parts don't need fine detail, I think printing them with 0.5mm filament and one outline would be quicker, but that would need a bigger nozzle.
The weight of the parts, not including the extruder, was only 730g. I printed the outlines at 16mm/s and the infill at 32mm/s, so it's hard to say the total time. Assuming an average speed of 24mm/s at 0.4mm diameter gives about 3 mm3/s. That would put the total time at about 65 hours. I did it as a background task over a few weeks. A lot of the parts were printed as experiments with heated beds.
Rods
I took me an evening to cut all the rods. The method I used was to nail a stop to my workbench to line up the rod against a metre rule.I then lined a piece of masking tape up with the correct measurement and wrapped it round the rod to mark the place to cut. I also wrote the name of the rod on the tape to make it easy to identify later.
A Black & Decker workmate makes an ideal vice to hold the rods while sawing. I rotate the studding until the thread lines up with the edge of the masking tape. That guides the saw to start in exactly the right place.
I used BZP for all the studding except the z-leadscrews, for which I used A2 stainless steel because it is smoother and generally straighter. I bought the rods from Farnell and even the BZP studding was very straight, a lot better than the stuff you get in B&Q. I also used A2 for all the bars.
It was very hard work sawing the A2 until I switched to a new blade and used Trefolex cutting compound. I am not sure which made the most difference, but I could then cut the A2 much easier than I had been previously cutting the BZP. I wish I had done that earlier, it would have saved a few hours.
Thick Sheets
The thick sheet parts are not really suitable for making by hand, particularly the squashed frog. They have lots of slots, which are hard to make without a milling machine or a laser cutter, etc.I am not sure exactly what the hole in the bed and the purge plate are for, so I made the bed a simple rectangle with four holes. I am using my own electronics, so I made the two circuit board plates to suite. I simply cut rectangles and I marked the holes and drilled them in the right place, so no need for slots. That just left the squashed frog.
I made a much simpler design with drill centres on it. There is no need for the bulging legs and sloping shoulders. I think they must be just to make it look more like a frog. Fine if you you are CNCing it, but a PITA if you have to make it by hand. Also the holes for the opto tab and the purge plate are mirrored for no apparent reason, so I made it chiral.
This just starts as a rectangle with some holes in it. Then the large slots are made with a saw thin enough to turn in the holes. The outer holes that mount the bearings can be round because they are in a a fixed place, dictated by the holes in the bed. The inner holes need to be slots because the bearings are adjustable. I just left them off the template and marked them with the bearings adjusted and in place.
I made the sheets from 3mm Dibond, which is below the recommended thickness, but seems stiff enough. It is also light weight and very easy to machine.
Thin Sheet
I didn't have any optos, so I used micro switches for my end stops, hence didn't need any thin sheet parts. I simply attached them to the bars of each axis with P-clips. A little RepRapped bracket would be better but I was building this in a hurry, so had gone into bodging mode at this point!They seem to have sufficient repeatability and certainly will when I replace the electronics with my new design, which will know the motor phase, reducing the uncertainty by a factor of 32. It is the same switch that I have used on the z-axis of HydraRaptor, which has proven totally reliable. They seem to be this one from RS, not cheap.
Belts
These were easy enough to split but, because the reinforcing wires run in a spiral, the blade tends to follow one for a while before managing to cut through it. That leaves a ragged edge with a bit of wire sticking out.I didn't understand the rationale for slackening the belts until you just don't see backlash when moving one motor detent. I am microstepping anyway, so a motor detent is not significant. I made my belts good and tight.
Snags
I had a few snags with the mechanical assembly: -The x-axis spacers are too short. The STL files are 5mm shorter than the parts in the STEP assembly. That caused the motor to clash with the nuts on the 360 bearing.
The 180 bearing at the other end was about 10mm from where it should be.
A simple fix was to slide the axis along leaving a 10mm gap to the spacer, the only problem remaining is that the spacers rattle at certain step rates.
The STEP model shows this gap should be only 5mm, but I have been unable to find the discrepancy. My rods and inspection distances are correct and the ends of the rods are flush with the clamps, as they are in the model.
The bed springs seemed to be too long to compress to the length of the bed-height-spacer-31mm_1off, which is not actually 31mm, but 29mm, so I don't know what gives there, I just spaced them a bit higher.
The bolts in the z-bar clamps are too long to allow the bearing to be inserted. I replaced them with shorter ones.
Similarly the bolts in the x-carriage get in the way of the extruder I fitted.
The J3 jigged distance did not seem correct. The distance between the y-bars is set by the J2 distance and the 3 nut spacers.
Extruder
I used Wade's extruder design as I didn't have time to adapt any of my own.The gears work well, with very little backlash, but the small one has some movement on the motor shaft. It is just a press fit with a flat on the shaft. I need to redesign it with a captive nut and grub screw.
I didn't have a suitable M8 shoulder bolt so I made one from brass by attaching a nut with a pin through it.
I hobbed it with an M3.5 tap. I haven't measured the grip, but I get the impression it is not as high as Wade gets, I am not sure why.
For the bottom half of the extruder I used some parts that Brian was looking for volunteers to test for him.
The insulator is made from PEEK with a PTFE liner. The idea being to get the strength of the PEEK and the slipperiness of the PTFE. It seems to work well with PLA, which is all I have run through it so far.
The barrel is long because it is designed to take nichrome, but I just screwed it into a block of aluminium with a vitreous enamel resistor in it.
This was left over from a previous experiment. I have now moved onto a smaller resistor size, so this block could be smaller. The barrel could be a lot shorter with this arrangement and that would give less ooze and less viscous resistance.
The extruder works well with PLA. The main problem with it is that it mounts at right angles to the x-axis, so the motor severely restricts the maximum height of the z-axis. Another issue is that to remove it you have to remove the motor to get at the bolts. To remove the motor you have to remove the big pulley to get at the motor's bolts, to do that you have to remove the pinch wheel assembly. I.e. to remove the extruder you have to completely disassemble it!
Electronics
To get up and running quickly I used the same electronics that I use on HydraRaptor. The only difference being that I used MakerBot V3 stepper drivers. These use the A3977 chip and give x8 microstepping. That gives an axis resolution of 0.025mm, but more importantly gives nice smooth running.When the weather was exceptionally dry I found they are very sensitive to static. A discharge to any part of the machine would cause the A3977 to shut down its outputs and draw enough current from the 5V rail to cause the 100mA regulator to current limit. The red LED on the power rail goes dim. Powering off and on again fixes it and there doesn't seem to be lasting damage. I suspect that might not be the case if the 5V rail was not current limited. Apparently the only way to fix it is to add external Schottky diodes. That is very disappointing as one of the nice features of the chip is that it is supposed not to need them. I will investigate further to see if all eight diodes are needed before making my own board.
Firmware
I used the same firmware as HydraRaptor. I just added some compile time conditionals to cope with two pin outs and a different IP and MAC address for each machine. I also had to change from 16bit to 32 bit positional commands because the axes are bigger.Software
I used the same Python software as HydraRaptor but I had to re-factor it quite a lot to support both machines. I added a class to represent the Cartesian bot which holds the axis resolution, direction, maximum speed and acceleration plus the IP address. I also added a class to represent the extruder controller as I have calibration values unique to each board. I already had classes to represent thermistors and extruders.I can run both machines at the same time from one PC and, because I only use the Skeinforge output for the toolpath, I can use the same sliced files for either machine. This is despite the fact that they run at different speeds and are loaded with different plastic.
Results
So here is the finished machine: -And here is a video showing it being tested: -
I am running the X & Y motors at about 0.75A and Z at about 1A. I have set the maximum XY speed to 100mm/s, but I think it could go a lot faster. Z only goes at about 5mm/s because not only is it a threaded rod drive, but it is geared down by the belt and pulleys!
I haven't printed a lot yet, but so far the results look as good as they do from HydraRaptor. The next thing to do is add a heated bed and try ABS.
Wednesday, 17 February 2010
PMMA on PI
Previously I described how I made some lamp shade clips for some friends from PMMA (Acrylic). Unfortunately the clips got lost in the post so I had to run off some more. I used a sheet of acrylic as the bed the first time, but since then I have developed my magnetic bed with PI (Kapton), so it was an interesting experiment to see if PMMA would stick to PI.
The originals were made with the bed at 100°C, but the insulating effect of 4mm of PMMA gave a surface temperature of only~85°C. That was sufficient to form a partial weld strong enough to resist warping. My first test was with the bed at 100°C, but that came loose after a few layers. With the other plastics I have found I need a higher temperature on PI because it does not form a weld. It sticks by some magic that I don't understand, possibly Van de Waals forces.
I tried again with the bed at 130°C and this time it stuck well but was easily peel-able by bending the bed. So another plastic that works on hot polyimide.
I have also been doing multi-part builds one layer at a time, something I hadn't dared to do until recently because my previous extruders were not reliable enough to risk a bed full of objects.
If you get the height just right on the polyimide bed the first layer comes out almost perfect. You can actually make one layer thick objects, i.e. 0.3mm in this case.
These came out very well.
I arrange multiple items by reading the STLs into AOI and orienting and positioning them. I then union them together in pairs and then union all the unions until I have a single object. I then convert that to a triangle mesh and export it as a GTS. If I don't convert first I only get one object in the GTS rather than the composite. I then slice as one object.
These springs show a very rare bug in Skeinforge or my code where it does a move with the extruder on. That is the only time I get any string.
Here is an assortment of smaller parts :-
It is best to group the taller parts together so when it gets to the higher layers the head does not have far to travel.
There were so many in this build that it overlapped the hot part of the table, so a few corners lifted a bit. I think ideally the table should be a bit bigger than the movement to keep some warm air around the objects. Perhaps a wall around the edge would keep some heat in.
I did have the crazy idea of building a wall around the objects as they are made so that there is a small gap of trapped hot air around them. I.e. the machine builds a disposable cocoon around the object to act as a heated build chamber. It would be a bit wasteful of plastic of course but it could be made from a cheap paste if we had a second head.
The originals were made with the bed at 100°C, but the insulating effect of 4mm of PMMA gave a surface temperature of only~85°C. That was sufficient to form a partial weld strong enough to resist warping. My first test was with the bed at 100°C, but that came loose after a few layers. With the other plastics I have found I need a higher temperature on PI because it does not form a weld. It sticks by some magic that I don't understand, possibly Van de Waals forces.
I tried again with the bed at 130°C and this time it stuck well but was easily peel-able by bending the bed. So another plastic that works on hot polyimide.
I have also been doing multi-part builds one layer at a time, something I hadn't dared to do until recently because my previous extruders were not reliable enough to risk a bed full of objects.
If you get the height just right on the polyimide bed the first layer comes out almost perfect. You can actually make one layer thick objects, i.e. 0.3mm in this case.
These came out very well.
I arrange multiple items by reading the STLs into AOI and orienting and positioning them. I then union them together in pairs and then union all the unions until I have a single object. I then convert that to a triangle mesh and export it as a GTS. If I don't convert first I only get one object in the GTS rather than the composite. I then slice as one object.
These springs show a very rare bug in Skeinforge or my code where it does a move with the extruder on. That is the only time I get any string.
Here is an assortment of smaller parts :-
It is best to group the taller parts together so when it gets to the higher layers the head does not have far to travel.
There were so many in this build that it overlapped the hot part of the table, so a few corners lifted a bit. I think ideally the table should be a bit bigger than the movement to keep some warm air around the objects. Perhaps a wall around the edge would keep some heat in.
I did have the crazy idea of building a wall around the objects as they are made so that there is a small gap of trapped hot air around them. I.e. the machine builds a disposable cocoon around the object to act as a heated build chamber. It would be a bit wasteful of plastic of course but it could be made from a cheap paste if we had a second head.
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